The blog may have been off line for a holiday break for a couple of weeks but there has been plenty happening in the meantime.
Headline news has been the arrival at Preston last Wednesday of FR 25’s boiler, albeit as a kit of parts. Tim received news by email of the need to move the boiler from Stockton whilst he was out of telephone contact on holiday in Cornwall. It took three journeys to the top of the local hill to get reception and organise the move, which was done with great help from Jacqueline at Northern Steam Engineering who made the arrangement for a hi-ab to transport the components as a crane could not be guaranteed to be present at Preston. In the end, the boiler was loaded a day early last Tuesday and so made an early arrival at Preston on the Wednesday morning. Fortunately, the former Furness Railway bogie bolster had already been shunted into position and the hi-ab departed back off to the north east at 10.45.
The other components were placed in the car park and will need to be moved this next Wednesday.
During the ensuing shunt moves there was a rare sight captured with FR 20, the FR bogie bolster and two boilers which have adorned ex Furness Railway locos.
Work has started on the overhaul of FR 20, with the ceremonial draining of the water from the boiler on the Wednesday the 18th July.
Last Friday Tim started the job of cleaning down the driving wheels and John Davis commenced the task of de-scaling the coal space in the tender.
Fred also took the opportunity to reprise his role as principal cleaner of FR 20’s smokebox!
John Dixon has continued to undertake woodwork repairs to the Great Eastern Royal Saloon and is seen here repairing one of the step boards.
Keith has made more progress with Wootton Hall‘s tender and has been fettling up the recently shot blasted tender hanging plates.
There has been more riveting of the tender frames and Keith is seen here pondering the next move in the restoration.
Cumbria has been out of traffic at Embsay recently owing to excessive amounts of from steam passing through the regulator when it was closed. Many people have looked to solve the problem and Andy Booth appears to have come up with a likely answer requiring a small modification. Things were looking much better yesterday and it is hoped that it will be back in traffic soon. It is also hoped to undertake a formal hydraulic on 5643 this week. Keith and Fred paid a further visit yesterday and Keith is scheduled to return to Embsay tomorrow (Tuesday) to start the process of re-assembly.

Elsewhere at the Ribble Steam Railway a start was made last Wednesday on fitting out the new children’s playground. Groundworks are scheduled to take place from next Monday.
The RSR’s Sentinel 0-4-0 Enterprise, which is in the museum as part of the Sentinel display, has received a wrap depicting events over the last 50 years.
The boiler for Hunslet 0-6-0ST Glasshoughton No. 4 arrived back from Llangollen last Wednesday.
Finally, an impressive 100ft long model tram layout returned to the RSR this last weekend and Tim is seen here doing some moonlighting, driving trams in between driving the steam service yesterday!
Adrian can be seen here starting the process of applying red oxide to the cleaned up cab.
Meanwhile Alan seemed pleased with the results of the shotblasting.
Fred and Roger finished the job on Friday, but not before the cab had unfortunately been sprayed with the first rain in weeks!
The shotblasters should be returning this Wednesday to tackle the cab roof and also another cab that does not belong to the FRT.
Saturday was a little quiet (something to do with a football game!), but plenty of people, including many members and friends, came along to say “Goodbye” on Sunday. Coincidentally, Neil was able to spend his first full day on the footplate at Preston that day as he looks to regain his fireman’s ticket – at least he had a loco that he knew from times past.
Sadly, after handling the train service and rake of three coaches without fuss, FR 20 retired to the shed at the end of service on Sunday afternoon in steam for the last time for a while. As Tim put it at this point: “finish with engines”. We know from the large amount interest on the internet that everyone is willing the FRT to get the loco back in traffic as soon as feasibly possible.
John is seen here cleaning out a droplight sill prior to reassembling it. Roger has started the job of sanding down and priming parts of the buffers and couplings.
Keith has brought back some of 5643’s components from Embsay for fettling and Fred is seen here on Friday cleaning up the regulator quadrant. Keith was due to go over to Embsay on Sunday as he looks to get 5643 back in steam as quickly as possible.
In the meantime, Keith has been lining up Wootton Hall‘s tender axleboxes with the overhauled tender frames, seen here at work. A further riveting session is planned for Thursday.
Alan Ogden has once again been tackling the instruments and smaller electrical items on Fluff and is seen here with a refurbished switch box.
Ade, Alan and Howard have been hard at it in their efforts to remove the final spring hanger pin on Caliban‘s frames. Suffice to say that plan Z didn’t produce immediate results, but lots of sweat and toil were duly expended and victory was eventually achieved.
It is pleasing to be able to report that the riveting session on Wootton Hall the previous Thursday had seen approximately 50 rivets installed, and evidence of a neat job is seen in this photo of a newly riveted bracket on the front portion of the frames.
Backing plates for the tender cab steps have also been bent to shape.
And a newly fabricated and shaped plate is seen here on the frames in front of the boiler.
Alan, Tim and Pete Skellon successfully made it to the Bolton Station Community Gala on Saturday and, would you believe it, played railway songs in the bus interchange for half an hour! Must have been rail replacement songs! Both Alan and Pete had been disorganised in forgetting to take their mobile phones with them, but between you and us Alan also forgot to take a set of teeth – but we won’t tell anyone, will we?
Ade failed to score with Caliban‘s last spring hanger pin last Wednesday and is now looking for a plan Z for this week. We will, as ever, keep you posted.
There is more varnish on GER No. 5 with still plenty more to apply once John Dixon has finished filling in all the remaining cracks in the woodwork. Meanwhile Mike and Paul Newton have been working on a plan to create a replica works plate for Rachel, Ken Nuttall’s petrol Simplex at Haverthwaite, for Roger who has been working on it for some time now.
John Dixon has been moving around the Great Eastern Railway Royal Saloon No. 5 filling in cracks on the teak panels whilst Mike Rigg has repaired one of the window frames.
Tim has continued the task of applying gold size and a first coat of varnish, which has been completed on the north side and east end.
Adrian spent Wednesday trying to drill out the last remaining spring hanger pin on Caliban, but to no avail so far. So plan B is for next Wednesday, although Ade hasn’t yet told us what that may be.
Howard has been trying to release the retaining screws on top of the spring hangers and he is seen here with David applying plenty of pressure on a stubborn screw.
Meanwhile Keith has been doing some more drilling on Wootton Hall‘s tender frames and is expecting Matt Gervis to appear on Thursday to start fitting some rivets. The NDT man is also expected this week to test the tender axles.
Outside the shed John Davis has been painting the mess room roof and, with the assistance of Fred, the outside is looking much cleaner in readiness for painting.
A 1949 Duple bodied Bedford made an appearance for the RSR’s Beer and Cider Festival over the weekend, but unfortunately Owd Sue, as she is known, succumbed fairy early in the proceedings owing to the failure of a lift pump. A replacement bus was supplied very promptly by Coastal Coaches.
Finally, we include a photo taken on the 27th May of Alison with one of her cream teas.
In the workshop there was a marked step forward on the (not so) mini project to remove the remaining extremely stubborn spring hanger pins from Caliban‘s frames. A further four pins were removed with the aid of an air powered hammer. Ade and David Starkie are seen here in action. Unfortunately, the air compressor sprang an oil leak and one pin, which has so far shown not one iota of movement, is still left to be extracted.
Sanding of the exterior woodwork of the Royal Saloon GER No. 5 has been completed and John Dixon is working his way around the coach with the wood filler. Tim has therefore been able to start the process of applying gold size, the effect of which can be seen by the accompanying photo, where the upper panels have received the gold size. Almost the whole of the north side of the vehicle has now been treated and more progress is anticipated this next week.
Outside the shed, there has been good progress on preparing the exterior of the mess room for painting. Fred had started the job the previous week and Paul Newton and John Davis are seen here on the roof applying the full force of the power washer. More red oxide on the exterior had appeared by the weekend and it is hoped to be able to continue this progress whilst the weather holds fair.
Furness Railway No. 20 made a return to steam at the RSR over the Bank Holiday weekend, operating successfully over the Saturday, Sunday and Monday. The tender had been lowered back on to its rear wheelset the previous Wednesday after attention to the rear right axlebox. We are pleased to report that the axlebox showed a significant improvement in performance and, whilst still warming up over a period of time, was nothing like as bad as had been experienced at Shildon during FR 20’s latter steamings there. No doubt the axlebox will get further attention during the locomotive’s forthcoming overhaul.
As mentioned in last week’s blog, the main task at this last Wednesday’s working party was the jacking up of FR 20’s tender to attend to an axlebox which had been showing signs of warming up during the latter days of its operation at Locomotion, Shildon. Once the axlebox had been dismantled it became clear that both the bearing and the journal had, for some reason, become scored. Also, the bearing had become too good a fit, not enabling oil to circulate and lubricate the interface between bearing and journal.
Alan, meanwhile, took the bearing aside to remove some of the brass in order to give some more lead towards the top of the bearing, so allowing more oil to circulate.
The oil pad showed signs of wear to the rivets, which suggested that these had come into contact with the journal. Some horsehair was retrieved from store with a view to substituting this instead of the oil pad when the axlebox is reassembled. The engine, incidentally, already has horsehair in its axleboxes and this seems to have worked well in the past. All being well, FR 20’s tender will be back on its feet on Wednesday and it is proposed that it will be in service on the RSR over the Bank Holiday weekend.
Work also progressed on Caliban where a further spring hanger has been freed off, much against its will. Only another five to go! Howard is seen here tackling the next one.
Keith has been making the most of his retirement, as can be seen from this photo of new steelwork between Wootton Hall‘s tender frames.
Meanwhile, Tim, Paul Newton and John Davis continued the job of sanding down Great Eastern Railway Royal Saloon No. 5 whilst John Dixon filled and sanded down the various cracks in the teak panels.
The job continued on Friday when Fred and Roger joined Paul and the two Johns, with the task now well on the way to completion.
That’s just as well for the work really does take it toll, numbing both fingers and mind!
We forgot last week to congratulate Keith on his retirement from his job with Ribble Rail on the 4th May. Needless to say, Keith is making the most of his new found leisure time to progress the tender frames for Wootton Hall. He is seen here drilling a brace section that will support the vacuum cylinder.